Mein Hexa ist fertig und fliegt gut meine ich, wenn ich die logs Auswerte kommt dieses dabei raus:
Log File C:/Program Files (x86)/Mission Planner/logs/HEXAROTOR/1/2016-03-17 19-33-16 7.bin.log
Size (kb) 29237.6298828125
No of lines 353394
Duration 0:15:32
Vehicletype ArduCopter
Firmware Version V3.4-dev
Firmware Hash 4bf3ec0e
Hardware Type
Free Mem 0
Skipped Lines 0
Test: Autotune = NA -
Test: Balance/Twist = NA -
Test: Brownout = GOOD -
Test: Compass = GOOD - mag_field interference within limits (7.53%)
Test: Dupe Log Data = GOOD -
Test: Empty = GOOD -
Test: Event/Failsafe = GOOD -
Test: GPS = GOOD -
Test: IMU Mismatch = FAIL - Check vibration or accelerometer calibration. (Mismatch: 4.88, WARN: 0.75, FAIL: 1.50)
Test: Parameters = GOOD -
Test: PM = NA -
Test: Pitch/Roll = NA -
Test: Thrust = NA -
Test: VCC = GOOD -
Was kann das IMU Missmatch sein ?
hier noch die passende Logfile:
Anhang anzeigen 2016-03-17 19-33-16 7.bin.log.zip Anhang anzeigen 2016-03-17 19-33-16 7.bin.log.zip
Vielleicht kann mir ja einer der Experten nen Tip geben.
Danke !!
Log File C:/Program Files (x86)/Mission Planner/logs/HEXAROTOR/1/2016-03-17 19-33-16 7.bin.log
Size (kb) 29237.6298828125
No of lines 353394
Duration 0:15:32
Vehicletype ArduCopter
Firmware Version V3.4-dev
Firmware Hash 4bf3ec0e
Hardware Type
Free Mem 0
Skipped Lines 0
Test: Autotune = NA -
Test: Balance/Twist = NA -
Test: Brownout = GOOD -
Test: Compass = GOOD - mag_field interference within limits (7.53%)
Test: Dupe Log Data = GOOD -
Test: Empty = GOOD -
Test: Event/Failsafe = GOOD -
Test: GPS = GOOD -
Test: IMU Mismatch = FAIL - Check vibration or accelerometer calibration. (Mismatch: 4.88, WARN: 0.75, FAIL: 1.50)
Test: Parameters = GOOD -
Test: PM = NA -
Test: Pitch/Roll = NA -
Test: Thrust = NA -
Test: VCC = GOOD -
Was kann das IMU Missmatch sein ?
hier noch die passende Logfile:
Anhang anzeigen 2016-03-17 19-33-16 7.bin.log.zip Anhang anzeigen 2016-03-17 19-33-16 7.bin.log.zip
Vielleicht kann mir ja einer der Experten nen Tip geben.
Danke !!